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Atlantic Shore Line Locomotive 100
Curatorial Report No. 7
1 April--9 September 2007
by Donald G. Curry, Shop Manager First, let me make an apology for the long time since you last received a curatorial report on this project. The excuses are:
1. Its our operating season so we need to spend a lot of time on keeping the fleet running.
2. Its painting season so we do that in the un-heated areas.
3. There are many other projects in process simultaneously, 5 to be sort of exact, that need our attention.
However, we know you will soon agree that the project is far from dead. In fact, its extremely alive and well,
especially for these past three weeks.
Traction motors All four have been completely overhauled by A.C. Electric at a cost of approximately
$13,500. This includes installing the rebabbitted motor bearings. Because the truck frames are not complete the
motors are being stored at no charge by A.C. and will be delivered when the truck work is completed.
American Power Service, in Georgetown, MA did the rebabbitting and Dean Look machined them to the
diameters requested by A.C.s Shop Supt. Roger Paradie. They are now installed in the motors, all of which
have been test-run.
Trucks We have deliberately left most of the one truck together with the exception of the wheel-and-axle sets, the motors, journal boxes and equalizers. All of these parts are ready when the time comes for re-assembly.
When a project spreads out over time and personnel change, there still is first-hand evidence of how things
were. The first truck has been partially assembled by Bill Pollman and Randy Bogucki. This includes the two
new transom channels, arch bars, truck pedestals and wear plates, and all new bolts. The equalizer bars with
associated spring seats were also re-assembled. This turned out to be quite a puzzle (Imagine one with 150 lb.
pieces!) because the hole spacing on them varied. As we assemble everything, we put caulking on mating
surfaces as well as Never-seeze on bolts, just in case they have to be disassembled.
Meanwhile the beautiful double-elliptic springs have arrived and are ready to do into place. Also the journal
bearings (brasses) have been received from Mid-West Locomotive and Machine Works. They were babbitted
by American Power Service but still need to be machined. Dean is uncomfortable doing the job so is working
with some a machinist from his old stamping grounds Down East, who says he can do the job. Dean also said
he would very likely to have done it if our Milwaukee horizontal milling machine were set up again.
Fortunately the motor axle (suspension) bearings were not badly worn and can be re-used, possibly with some
repair of the dowel pin holes which tend to work to an oval shape.
Truck work largely stopped when the weather got warm enough to do outdoor work.
Body bolsters In our last exciting episode, Dean Look had his welding torch poised and ready to weld up the
rounded ends of the top member of the body bolsters. He did than and ground away the excess metal and they
look exactly like the originals.
Then it was necessary to drill the holes in the bottom plate to line up with those in the top plate through which
the bolts holding the side bearing castings, which also hold the bolster together, must run. Because the plates
slope up from the bottom where the center bearing is bolted, to above the side bearing mounts, it meant drilling
into an angled plate without having the drill walk. As mentioned in the last report the hollow Hougan bits
will move right across the face of a piece of steel unless the magnetic drill press which turns them is very
solidly anchored against thick steel. After some thought, a jig was created using a surplus piece of 1 x 8 in. plate
as a base and the drilling proceeded with no walking or snapping of expensive bits.
Then the primed pieces were given the requisite coat of Awlgrip Super Jet Black and everything was bolted
together. For several months the no. 1 bolster assembly was set on the shop floor under its future location but on
30 August, it was raised against the waiting longitudinal sills for its trial fitsome change from the nearly
rusted-away original. The no. 2 end bolster is drilled but is awaiting the disassembly of the original bolster
which contains the center and side bearing castings.
A Family Affair At the beginning of the summer we received an E-mail from a Susan Dow speaking of her
sons intense interest in railroads and trolleys and how it would be great if he could work on restoring one with
his grandfather, who is a first-rate cabinet maker, some time this summer. Time went by and nothing further
was heard until 13 August when we got a phone message. She, her mother and father and son were in near-by
Cape Porpoise and they were ready to come over and help out. I invited them to come right over and we all
introduced ourselves. Then I said, to Tom (Susans father), Are you related to Sterling Dow? Tom said, Yes,
hes my grandfather. So that made Susan his great granddaughter and Christopher, Sterlings great-grandson!
As I thought about what they would like to do over the next three weeks it became ever so logical they should
work on 100. (Sterling Dow was General Manager of the Atlantic Shore Railway and York Utilities from
1918-1924!!) Tom said he had absolutely no idea of the familys trolley connection.
So, I said, Ive got just the project for you! As you will see, during their all-too-short visit, 100 rapidly
transformed. Of course we didnt want to leave Sue and Christopher out of the action. Chris would assist his
grandfather in addition to doing a BAM. Sue would work on much needed upgrading of the displays on the
Shop Visitors Gallery.
These displays were large rectangular wood frames 14 x 40 in. with glass, which can easily hold four 8 ½ x 11
photos. So we had a number of photos laminated along with captions 5 of which have been installed on the
visitors gallery, either on top of the box or on the wall. Sue ran out of time so there are a number more to do. Of
course we want to have one featuring the Dows at work and have the necessary photos to do that.
Making the chips fly - As soon as I discovered the family connection I knew just what Tom would do well:
rebuild the wood structure of ASL 100. It was poised and ready except for one thing: Barnstormers! still hadnt
delivered the long-promised vintage southern yellow pine. Sue volunteered to go to Portland, where they are
located in the old Union Station train shed, to get the wood in her Ford Explorer. We made phone contact with
John Rousseau, the owner and soon she was off, returning an hour later with front wheels barely touching the
road and vintage SYP hanging long out the tail gate. Now we could do something. (She had been given the
understanding that we now had all the SYP we were supposed to get except the long side sills, but it turned out
not to be quite so.) Still Tom had all he needed to keep him very busy.
Step 1. Make the sills solid and even. Over time the 6 inner sills have twisted, rotted and drooped with the
weight of the coupler and weakening due to the rot. In our initial figuring of what was needed6, following along
with the style of repairs made by ASL/YUCo, we figured we would need to remove and replace 3 inches of the
top of the six inner sills and 3 in. from the bottom of at least two. So, for the no. 1 end we ordered eight 3 x 5 in.
pieces of SYP in lengths of two to eight feet, depending on the condition of the sill to which they were being
fastened. In some cases this was simply replacing the repairs made by ASL/YUCo which and deteriorated and
for others it a new repair. By using a nail and/or screwdriver, it was possible to poke and the sills to determine
how solid they were.
Tom was always concerned that we werent going to leave anything of the original sills. (We had long
determined we would preserve the original inner six sills as intact as possible and, in no case, cut one
completely through.)
He made a jig from a 6-in. wide strip of plywood fastened to each side of the sill in question. This kept the saw
cutting the same depth through the entire cut. It was necessary to make many cuts about 1 in. apart across each
sill; then remove the remaining wood with a chisel. Because of the depth capability of the skill saw it took two
settings to reach the full 3-in. depth. He then evened up the surface with a belt sander using a coarse grit.
Step 2. Fasten the new tops (and bottoms). Here we used West System (two-part) epoxy with their 406 high
density filler. To keep it from running, even with the filler, which thickened the mixture, he had to apply waxed
paper to the glued-up joint, clamping it in place with wood scraps. The ASL/YUCo held the fillers in place with¾ in. square-headed bolts vertically down through the filler and sill. We are considering whether to do use bolts
in addition to the epoxy or simply depend on the epoxys strength. (Weve heard that it doesnt hold up well in
shock situations, as in coupling up to a railroad car. Anybody know anything about this?)
Step 3. Replace the missing end tenons. On the end of each sill are two tenons which hold the sills in line and
support the big end sills. The tenons range from 1 ⅜ in to 1 ½ in thick by 5 in. wide on the inner sills and about
3 in. on the outside sills. A number of them had deteriorated or were missing. We noted that some of the sills
had twisted during Laconias period of building 100. In order to keep the tenons in line, the horizontal surfaces
were made level but, because of the twist, they were actually slanted in relation to the sill. This took some
careful measuring.
Step 4. Replace rotted and hollowed-out interiors. When the locomotive operated, the first parts to move
were the trucks. Their force was then transmitted through the truck bolster, the truck center bearing, the body
center bearing, the body bolster and finally the body. Holding this all together were the twelve three-quarter in.
diameter by 14 in. long square-head bolts which ran down from the top of the sills through the top plate of the
bolster. (The end ones went through both plates which came together for their last few inches.) As the car
operated, great strains were put on these bolts and the wood surrounding them. As the wood aged, it shrank
somewhat allowing the bolts to loosen slightly which then allowed the bolts to work slightly-more and more
over time. At the same time, water worked its way down along the bolts, deteriorating the wood as well as the
bolts.
Originally the bolts very likely only had washers under their heads, barely enough to hold the structure solidly
together. So, at some point, ¾ in. x 6 in. plates with two holes were set in notches on top of the six inner sills.
The outer sills were reinforced with ¼ in. plate rough-cut with a torch, as were the ends of the inner pieces.
These served well as reinforcements until the end of 100s operating life.
However, when we removed these plates and their associated bolts, we found most of the holes in the sills had
greatly enlarged and needed to be filled. Using a specially purchased 4-in. shank with a 2 in. carbide cutting
blade router bit, Tom used a router to first cut away a notch across under side of the sill, similar to the one on
top. He made a guide frame which kept the router horizontal. Then he chiseled out the deteriorated wood in the
center of the sill, being careful not to totally destroy its longitudinal integrity. He fitted new pieces of SYP and
epoxy glued them into each cavitygigantic dental work.
The six plates on top of the sills plus a couple of small ones at the kingpin are in good shape only requiring
sandblasting, priming and painting. The outer ones may require replacement although we should be preserving
some of their rustic quality.
Step 5. Cutting the mortises and drilling for the through-rods. Although we have a large hollow-chisel
mortiser, capable of cutting the mortises, it would have been very awkward to manipulate the big end sill on
the router table as well and hold it in place. So Tom decided we should drill and chisel them. Using a big multispur
bit in the Rockwell drill press and hand chisel, this was done quite quickly.
Through each end sill run the four 1 ¼ in. steel rods which run from one end of the locomotive frame to the
other (about 30 ft. 6 in.) We purchased a 1 ⅜ in. ship auger bit to make the holes.
Step 6. Installing the body bolster As mentioned above, this critical piece of the locomotives structure was
bolted to the sills. Using a Masonite template, Tom bored 13/16 in. holes up from below through the top of the
sills. Then he and Dick Avy jacked the new bolster up against the frame and dropped the bolts right down
through where they fitted perfectly. The bolster now is temporarily in place for show but will have to be
dropped when we treat the surrounding wood and add caulking.
On 29 Aug. Barnstormers! John Rousseau finally arrived with the two 30 ft. 6 in., 5 x 11 ¾ in. side sills. Dan
Cohen was of invaluable assistance with Mr. Lifto, the truck with the hydraulic crane and flat bed, in getting
off the long sills. In fact, with Randy Leclair and Ed Dooks’ help, he slid each sill the full length of 100 so one
is positioned on the floor on each side, right below where they will eventually end up. Barnstormers! also
brought down the big end sill for the no. 2 end and the two 2 x 8 x 104 in. spacers which go across the top of the
body bolster through notches in the longitudinal sills.
He said the big timbers came from the bleachery at the Bates Mill in Lewiston, Maine. The other smaller
timbers came from a mill in Fitchburg, Massachusetts.
We did some more careful figuring and decided we had omitted two 5 x 8 in. x 120 in. fillers which are bolted
to the inside of the long outside sills under the cab. (We had thought they were a later addition, but after finding
the antique carriage bolts holding them in place and the porcelain tube, in one, leading the wire to the original
under-the-floor air compressor, we decided they were from day one.) Also, after studying the photos for thenth time, we determined we had forgotten two 2 x 6 ½ in. x 18 ft. trim beside the cab on top of each side sill,
also beside the cab. These run the entire length of the cab including the two hoods whereas the one above ran
only beside the cab itself.
Most of the timber has longitudinal cracks which do not detract significantly from its strength. We have
discussed whether or not to fill them. We probably wont except on the outer exposed surfaces. And even then,
not entirely. Given its age, the timber certainly has had time to stabilize but we are concerned about whether the
crack might open again and fall out. Its interesting to note visible splits on 100s outer sill even when it was
fairly new.
Still to come is the oak for the end decks and the pilot as well as a few more pieces of SYP: especially the filler
pieces for the sills on the no. 2 end.
The through-rods. These four 1 ¼ in. diameter x about 31 ft. rods extend through the end sills on each end of
100 and basically tie the locomotive together. The center two also go through the couple support blocks and
the top two of the four holes holding the coupler. These run straight though without any bends although they
were somewhat bent when removed. Because of their connection to the coupler casting, they took a lot of strain
and it appears the some of the ends of the rods may have been replaced by welding at some time or other. As
they passed directly through the wood they were corroded to the point their cross-section was diminished so we
decided to replace all four ends. Dean cut and threaded on the lathe, four pieces of 1 ¼ in. rod, ground one end
to a point and welded them on.
The outer rods pass through the poling pockets on each corner of the end sill, are horizontal as far as the bolster
on each end, where they are supported on a 4 x 6 block set on the bolster filler. Then they bend down about a
foot, to become horizontal for about 10 ft. before bending up and then horizontal for the other end. They bear
upward on some special castings (of which we only have one original of the four needed) which serve to hold
the center of the sill up, keeping it straight.
On most cars these truss rods can be adjusted by means of a turnbuckle in their center. However on 100, the
adjustment is via a large square nut on each end. It would appear that 100 remained quite straight for all of its
days, probably because of the strength of the eight longitudinal sills. These rods, although pitted over time, were
in good enough condition so they did not require any repairs. Randy Leclair removed the loose rust with an airoperated
C.R.U.D. disc tool. He then applied a coating of black Chassis Magic epoxy rust sealer. This will be
followed with Awlgrip Super Jet Black enamel.
Air compressor – 100s big GE CP 30 air compressor is still at A. C. Electric, in the process of overhaul. Some
time ago they removed its two main bearings and sent them down to us, feeling they were worn too badly and
their babbitt lining was badly cracked. Instead of bronze, these are steel shells, line with babbitt. Unlike bronze,
where the babbitt metal actually solders itself to the shell, in steel shells it is held in place by dovetail grooves
cut on the I.D. of the shell.
Don, Good morning,
We have inspected the air compressor motor and found that two bearings are defective, and need to be repaired.
I will send them with John (their driver) today so you can take care of them.
One bearing is a Crankshaft bearing (the short one) and the journal diameter is 2.7485 - 2.7490”.
This bearing should probably be bored to 2.755”.
The long bearing is the armature bearing (motor side) and the journal diameter is 2.2483 – 2.2485”.
This bearing should probably be bored to 2.258”.
These are only recommendations for the new bearing bore, and if anyone has a spec for them I would use it instead.
Regards, Roger P(aradie).
Norman Down, who lives in Georgetown, MA, where American Power Service, the company which did the
motor and journal bearings for 100, is located. We asked for estimates, either to re-babbitt and machine them to
dimension or just to re-babbitt the shells for us to turn them to the recommended dimensions. For both estimates
the cost was extremely high. Here is the E-mail which I sent to Dean Look regarding this:
ASL 100 compressor bearings: Possible scenarios
1. Do nothing and simply put the originals back as they are
2. Have American Power Service rebabbitt them and machine them ($2,012)
3. Have A. P. S. rebabbitt them and we machine them. ($1,007)
4. Have STM enter the babbitting field-much cheaper and much easier than 639’s armature bearings.
5. (If that doesn’t work) Machine new bearings out of bronze bearing stock. (Say about $200 or less for materials)
What is the opinion of the lead machinist?
His reaction was that both costs were outrageous but we had no alternative.
The next step was to determine what the alternative was, starting with bronze tubing from which we could
machine new, if not quite historically accurate, bearings. These would not be babbitted but would have oil
grooves cut in them. This turned out to be quite expensive too and you would have to purchase a 13 in. tube
even though one baring is only 3 in. and the other 6 ½ in. long. The alternative we have gone with is oilite
bearings from Bearings Specialty Company, which we will machine to exact size for about $200 for the two of
them.
The ‘one-hood’ photo. A week or two ago, you should have received a photo taken in the 1920s at the River
St. carhouse (were guessing) of 100 with only one hood. This was discovered by Norm Down in the STM
Library. We scanned it and got the details we needed from it. Phil Morse has subsequently taken it to a
company in Biddeford which specializes in photographic restoration for them to bring back to original
condition.
The wheels. P D & Y 108 was in the Shop recently being serviced for Pumpkin Patch. As it was there we noted
its interesting spoked wheels and realized these were probably the same type 100 had when it first operated on
the ASL. 108 came to the ASL from the P D & Y on a flat car sans wheels. ASL was scrapping the big
interurban cars so they had plenty of appropriate trucks.
The location of the locomotives.
More from O. R. Cummings. The new carhouse on River Street, Sanford, was built in 1923-24, using materials
salvaged from the coal pocket near Town House Junction. I do know that Nos. 100, 101 and 102 all were in
Sanford in 1927 and that the body of No. 101 was sold to a private party a few years later. You may recall
seeing it south of the Route 1 bridge over the B&M in Biddeford.
Yes, I do recall it well although I was too young and without the means to do anything about it. This was at
Underpass Auto Parts, often referred to by Seashore people as Underpass Overparts. It was used as a storage
shed, perpendicular to U. S. 1 about 30-40 ft. in from the road but clearly visible including 101 on the end. I
remember it was painted a sort of mud brown. I also remember seeing it burning as it was in the way of some
sort of improvement project.
Grouchy Mac did go there and get the two operators seats which he then installed either in 838 or 1391. The
actual seat folded in an upward direction. I think theyre painted a forest green.
The Color Match has been completed by Building Conservation Associated, Inc. of 580 High St., Dedham,
MA 02026 and their paint analyst, Brian Powell. Unfortunately we have not been able to visit them but do have
their detailed report. Their results may be somewhat underwhelming but theyre what you might expect on such
a work-a-day machine. Their report will be on a separate report to be sent shortly after this one. (This will make
it easier for my dial-up line to handle.)
Coal Stove – Thanks to a connection made via Jim Hamlin and the Maine Narrow Gauge RR, we now have
an appropriately sized cast iron pot belly stove.
The word is out Those of you who receive the Railway Museum Quarterly, published by the Association of
Railway Museums (A.R.M.) have seen the first of a series of articles they will run on ASL 100. We have
developed a very good relationship with Aaron Isaacs, the Editor of this fine publication. Here is his preface to
the story in the Summer 2007 issue:
According to the RMQ Reader Survey, published in the Fall 2006 issue, readers want to see more how
to do it articles on restoration. Nobody does a better job of reporting on a restoration than Donald Curry
of Seashore Trolley Museum. And nobody does a more thorough job of the restoration itself. By happy
coincidence, Seashore last year began the TEA21-funded restoration of Atlantic Shore Line (York
Utilities 1922-47) wood steeplecab locomotive #100 (Laconia 1906). RMQ will be publishing Dons
Curatorial Reports as they appear, hopefully until the project is complete.
In each Quarterly Isaacs has items about the multitude of railway museums all over the country which he has
visited. Often there has been a mention of Seashore, as well as the great photo of Cleveland 1227 on the cover
of a recent issue. Aaron regularly receives our Dispatch as well as copies of the curatorial reports such as this
but we seldom saw anything but an occasional reference to the restoration work we do. He said that it was
difficult to report on projects that spread out over many years. The reader doesnt see any obvious progress and
it can get to be as interesting as watching paint dry. He had been looking for a major project that wouldnt
stretch on for too long a time and ASL 100 was it. This came together as we spent an afternoon in the lobby of
the convention hotel in Sacramento at last years A.R.M. convention and were really pleased that we can
accommodate his getting the word out.
The near future. We were not planning on working on the underframe until heating season so Tom Dows
availability pushed that phase way ahead. A.C. blasted and primed a number of brake parts including the slack
adjusters and brake cylinder and hand rails. They have been painted black Awlgrip.
We would like to re-assemble the first truck and now have all the materials to do that. Dean Look is working
with a machine company in Machias, Maine to machine the journal brasses to fit the various diameters on the
ends of the axles. 
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